Man In The Maze

by Rich Luhr, Editor of Airstream Life magazine

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May 11 2013

Drilling a hole in the Airstream

I drilled a hole in my Airstream.

Of all the jobs to be done on the Airstream this spring, this one scared me the most.  Anticipating it was worse than building new cabinetry, worse than de-greasing the hitch & sanding off the rust, worse than laying inside the front compartment and re-wiring (I’ll tell you about that one later).

The backup camera I installed on the Airstream three years ago has been very useful, but I made a serious mistake when I put it on the rear bumper.  That location was easy to reach but far too low.

As a result, car lights and setting sun would create glare, making the camera useless at dusk or at night.  I found that I needed the camera much more while towing on the highway, for situational awareness (i.e., what’s happening behind me) than I needed it for actually backing up.  So losing the camera’s functionality because of glare was a real annoyance.

Also the low position gave me a great view of the stripes on the highway and the bumper grill of the car behind me, but not of cars further away.  Because it’s a “backup camera” the field of vision is very wide, like a fisheye lens, and so the useful distance range isn’t long.  To get any sort of overview of the traffic situation it needs to be mounted up above the roof of the average car.

I knew all this after the first season of towing, but I also knew that the only way to get the camera up where it belonged would require drilling a hole in the rear dome of the Airstream.  Not a small hole either, but a whopping 5/8″ hole to fit the cable connector through.  I have never drilled a hole in the body of the Airstream before.  It’s sort of a forbidden thing, in my book, because every hole is a new chance for a leak, a spot that must be maintained with caulk, and something you can never un-do.  Remember, I just had to deal with a 3/4″ hole that was drilled in the roof eight years ago for the original cell phone antenna.

At least that hole was up on the top where nobody can see it.  This particular hole was going to be right smack in the middle on a very expensive & very visible piece of shaped aluminum, where a virtual waterfall is created every time there’s rain.  If I screwed it up, I’d be looking at an ugly patch forever.

This may explain why I put up with the inadequacies of the camera mount for three years.

IMG_2161

With all the other projects completed, and perhaps a bit of bravery inspired by their relative success, I had no excuse to avoid this one any longer.  The re-routing of the cable was easy: it was already in the bumper compartment, and from there it took only two holes inside the rear compartment to run it up into Emma’s bedroom.  A four-foot length of plastic wire chase from the hardware store hid the wire as it ran up Emma’s bedroom wall, and then … I had to face the final cut, right through two layers of aluminum, some fiberglass insulation, and out to the cold, cruel world.

In a previous blog I wrote that you should think several times before putting a hole in the Airstream’s skin.  I thought about it for weeks, running through all the possibilities in my head to ensure there was no other way, and that I had a plan for every possible screw-up.  I ran a piece of blue tape down the centerline of the trailer from the clearance light to the license plate, measured and measured again, then dusted off the dome, applied several layers of protective tape on the aluminum, and drilled a small “test hole” 3/16″ in diameter.  (If this hole had been wrong, it would have been relatively simple to plug it up with caulk.)

It was right on the money, so I continued through larger drill bits, eventually ending up with the monster 5/8″ drill.  Emma didn’t make me feel any better about this when the drill poked into her bedroom and she shouted (through the closed window), “Wow, that’s a big hole!”

The camera is now in place, secured by a very high-bond double-sided automotive tape, and sealed with Vulkem 116.  I wish I had gray or black Vulkem for this, because the white caulk smears look stupid on the black camera mount, but eventually I’ll get my hands on some and re-do it.  In the meantime, it works and the view from the camera is much better.

So I drilled the Airstream, and survived.  But I don’t want to do it again anytime soon.

Written by RichLuhr · Categorized: Airstream, Renovation

May 07 2013

Customizing the Airstream again

After a good run of posting every two days for a while, I had to shut up and focus entirely on work.  I have been monumentally busy the past several weeks, but you don’t want to hear about that.  The most interesting part of it (Airstream-wise) has been finishing up the cabinetry project that I began before our last trip to California and Nevada.

Airstream Safari cabinet areaIf you haven’t read back that far, here’s a re-cap:  We wanted to get rid of the tired old laundry & microwave rack that we whipped up while full-timing, and make the area more functional.  I removed everything on the curbside of the trailer from the entry door to the refrigerator wall.  Originally this was a fold-out credenza with two huge chairs, as shown in the floorplan.

Those chairs took up too much space and we got rid of the first one before we had even towed a mile.  (As far as I know it is still serving as bachelor apartment furniture in Ohio.)  The second one exited while we were full-timing.  We stopped in Florida for a few days and a friend fabricated a counter extension to run along the curbside wall (atop a narrow shelf that isn’t depicted in the floor plan).  We bought a cheap wire rack at a housewares store and muddled the whole thing up into a storage space for a microwave and a small laundry bin.  This was a little crude but it worked for six years.

Eventually we started keeping our recycling in a little cardboard box behind this wire rack, and shoes began to collect beneath the rack.  Then we added a catalytic heater on the wall by the refrigerator.  Eleanor began storing water jugs on the floor behind the rack, too, and we noticed that the recycling bin was often too small.

The point of all this is that gradually we had modified the space to suit our style, and we had noted what didn’t work about it.  After eight years it was safe to conclude we had a clear pattern of use and our “wish list” was based on experience rather than infatuation.  So when Mike & I ripped up the old floor, rebuilding the curbside storage was part of the plan.

I finally finished it last Friday, and I’m very pleased with how it came out, considering that it was a mish-mash of old and new materials.  I tried to re-use as much as possible of the Airstream plywood because it’s very lightweight, and to keep the look somewhat reminiscent of the factory styling.  The fold-out credenza is still there, but it has been moved to a new location further forward and off the wheelwell.  (Kyle and I did that a few weeks ago, and you can see how it was done in the earlier blog entries.)

Added to it is a new microwave shelf suitable for a 1.2 cubic foot microwave, a shelf below the microwave for one of Eleanor’s large pans (probably a cast iron skillet), a black recycling bin that is twice as large as our old cardboard box, room for two 12-packs of canned drinks or four gallons of drinking water, space for the sink covers/cutting boards and a few paper bags, a much larger shoe cubby, the same laundry bin, and a semi-hidden storage shelf for small items like headlamps.

The big win of the whole thing is the huge new countertop, made of black walnut with four coats of polyurethane.  It measures 18″ x 71″ by itself (8.8 square feet), and gains another couple of square feet when the credenza is fully deployed.  With three people in an Airstream and lots of things going on simultaneously, you can never have enough tabletop space.

The only thing we lost in this conversion was a magazine rack, which I will replace later when we find a wall-mounted rack that we like.  No rush on that.

To build this thing took far longer than I had hoped.  That’s partly because I didn’t make it easy on myself.  I didn’t like the standard steel L-brackets that were available at the hardware store, so I bought lengths of 3/4″ aluminum L-channel and cut brackets from it on the table saw, then drilled four holes in each of them.  They aren’t as stiff as the steel brackets but they are a lot lighter and still strong enough.  Plus, they’re aluminum—need I say more?

The Airstream didn’t make things easy either.  You can’t count on square, level, flat, plumb or tight in a travel trailer.  Things move, and they need to flex during travel.  So every cut was “custom,” to accommodate gaps, unevenness, and just plain awkwardness resulting from the original construction.  Eleanor and I had to stop several time and ponder ways to cover up unexpected issues.  I also had to design the cabinet to be light, strong, and yet able to flex a little where needed.  Overall, I think the job probably took about 30-40 hours and at least a dozen hardware store runs.

So it feels great that it’s done, and I think it looks pretty good.  Sure, the black walnut doesn’t match the original furniture color, but I don’t care.  It looks much more sophisticated than the original stuff.  Because the shelves are black melamine, and the microwave and recycling bin are black, they all tend to visually disappear so cabinet doors are unnecessary.  Eleanor even found black no-skid material to line her pan shelf.

For those who are interested, here’s a bit more trivia:  We used the 3/4″ aluminum L-channel to make trim edges and lips for the shelves. It’s screwed to the melamine with 3/8″ stainless screws.  The microwave is attached to the shelf with self-adhesive Velcro and a security strap (made of aluminum) screwed to the side.  A low vertical divider holds the recycling bin in place.  We found the little organizer (pictured with the headlamp in it) at The Container Store.  The countertop, despite being solid wood, weighs only 19 pounds.  The entire structure weighs about 35 pounds, not including microwave, which is probably less than the original furniture and the two chairs we pitched out.

The key here is that this design suits our way of life when we are traveling.  We need convenient, reliable, practical, and durable stuff.  We aren’t glampers or weekenders, we’re long-distance travelers and we live in our Airstream for months at a time.  Your needs will probably be different.  Customizing your Airstream is just like customizing your fixed-base home: everyone has their own needs.

I have never met a full-timer or long-distance Airstream traveler who hasn’t modified their Airstream quite a bit.  Even people with brand-new trailers do it.  So if you haven’t yet, my advice would be to think about what you do, what you carry along with you, what you most feel is lacking in your interior, and starting planning a few small customizations of your own.  It’s easy to start with something as small as an organizer or a hat hook.  But beware—despite the many hours this latest project took, I can tell you that modding the Airstream is addictive.  There will be more in our future.

Written by RichLuhr · Categorized: Airstream, Renovation

Apr 27 2013

Grease is the word

I haven’t been looking forward to this most recent Airstream job.  For a couple of years the A-frame on the Airstream (the front part, for those of you who don’t have a trailer) has been looking pretty ratty.  Paint chips from rocks have turned into unsightly spots of surface rust, and the orange paint of the Hensley hitch has faded, then gradually fallen off, leaving large patches of rust.  The paint on the top of the power hitch jack has chipped off too.  It’s getting embarrassing, like the interior floor was before we replaced it last month.

The problem with the job of repainting the hitch and A-frame is that there’s a ton of prep work and it’s messy.  The Hensley is loaded with grease, which over the years has congealed with dirt and coated not only underside of the hitch itself but also the chains, coupler, and about a third of the A-frame.  After removing all the hitch parts with the assistance of Mike, we dumped them into a large tub and degreased everything with industrial-strength degreaser and heavy brushes, then washed everything.  This job took about an hour, and by the end of it much of the black grease was transferred to our bodies and clothes.

Then we scraped the loose paint off with metal scrapers, and got the surface rust off with a wire brush attached to the power drill, leaving a surface of remaining paint that resembled a cracked dry lake.  It was not pretty, but it was already an improvement over what was there.  It really needs a good sandblasting and powder coating, but I’ve decided I will do this quickie scrape and re-paint just to get another year or two, and then I’ll take the whole thing into a professional shop for a proper & smooth job.

The A-frame was less of a problem because Airstream used real paint (rather than that orange stuff that Hensley uses).  It held up very well over eight years of heavy use and many miles.  We only needed to touch up spots with the wire brush (after washing), and then wash again to remove all the dust.  It should paint up nicely.

IMG_2131After a lot of consideration, I’ve decided to paint the entire A-frame area in flat black.  The Hensley parts will also be black, except the part that was orange which is now a metallic pewter.  Black hides the grease a little better, and it’s an easy color to match for touchups.

Those of you who own Hensleys might be wondering if I’m going to put the stickers back on.  I have an entire set of replacement stickers, including the serial # label, but I’m going to keep them on hand and install them after the hitch is professionally stripped and coated.

You might recall that I complained of our LED lights flickering when the water pump was running.  I had considered several possible causes and solutions, including using heavier gauge wire to the pump, and adding a capacitor.  I realized that all the solutions were aimed at the same symptom: voltage drops when the 12 volt electrical system was heavily loaded.  And since nobody else with the LED lights seemed to be having the problem, it seemed most likely that I should try to find the cause of the problem rather than trying to patch it.

IMG_2132With that in mind, the most obvious place to look was the main trailer 12v ground, which is (on my trailers) is located under the main frame on the street side, just in front of the spare tire.  There’s a fat bare copper wire that runs to a little copper clamp that is in turn bolted to the frame. Since we were in that area with the wire brush, I disassembled the clamp and found quite a bit of corrosion on the copper and the steel frame.  I brushed everything back to shiny and reassembled, then tested, and voila!  no more flickering lights. I’ll coat the area with dielectric grease to reduce future corrosion.

We used to know when the main ground needed cleaning because the Actibrake disc brake actuator would suddenly stop working.  This happened a couple of times (Four Corners)  (FL panhandle) and I got used to doing roadside clean-ups of the ground wire.  The replacement Dexter brake actuator we have now doesn’t seem to be as sensitive to low voltage.  So now the LED lights are our warning signal. I think as warning signs go, flickering lights is far better than having no brakes.

The next job will be to paint everything.  This time of year we get a breeze almost every afternoon, so we’ll either paint this evening around 6 p.m. if things have calmed down, or early tomorrow morning.  Then, re-assembly, re-greasing, and adjusting of the Hensley.

In between major jobs like this I’m working on the cabinetry and other small tweaks too.  For example, yesterday I replaced four bellypan rivets with the big “buttonhead” ones because the pan was starting to come loose in the back. I also fabricated a small plumbing chase from leftover pieces of black walnut, to replace the factory one.  The list of Airstream jobs that was a page long is slowly shrinking, and two of the four “big” jobs are nearly complete, so although time is short I think we’ll be ready to go to Alumapalooza in three weeks.

Written by RichLuhr · Categorized: Airstream, Maintenance

Apr 25 2013

A sticky subject among Airstreamers

In the Airstream universe you will find a curious phenomenon: passionate debates about caulk.  That’s because the constant movement of all parts on the road causes all travel trailers to leak eventually, and a good caulk is our first line of defense against rain penetration.  Rather unfairly, Airstreamers get more of this debate than owners of other brands, mostly because Airstreams have been around for so long, and so many of them remain on the roads after decades of use.

An Airstream might easily be re-caulked a dozen times over its lifetime.  In contrast, “disposable” cheap travel trailers tend to get chucked into a landfill when they start to leak because they’re starting to fall apart too. You don’t hear the owners of those talking quite so much about re-caulking. They’re busy re-financing.

Another reason Airstreamers love to talk caulk is the aluminum construction of an Airstream.  Silicone caulks don’t adhere as well to aluminum, so we tend to go for polyurethane caulks that are more expensive but stick like crazy and stay gooey for a long time. But what caulk is the “best”?

For decades, the gold standard of caulk for silver trailers was some gray stuff called Vulkem.  These days Vulkem is just a brand name, applied to various formulations of polyurethane caulk made by Tremco.  I use Vulkem 116 but you can also get TremPro 635 from the same manufacturer, and a few variants. Either way, it’s great stuff.  It’s sticky like hot salt-water taffy and adheres to aluminum like glue, once cured it flexes a lot without breaking its seal, and it’s designed for exterior use (only) so it’s UV-resistant and completely waterproof.

Finding the stuff is the problem.  Lots of online sellers offer it but since a tube is anywhere from $6-14 and shipping tends to add $7-9, you want to get it locally or combine it with another order to duck the shipping charge.  Locally it’s sometimes available through Home Depot or Fastenal, but here I couldn’t find it stocked anywhere so I had to order it.

OEM caulk starting to break down after 8 years?
OEM caulk starting to break down after 8 years?

You can always go to the local RV store and find products that claim to be roof caulk.  I’ve tried a few and had uniformly disappointing results, especially the “self-leveling” type.  Those RV-store caulks seem to be made for the disposable RV market, because they all break down in a few years under sunlight and start to crack, then leak.  You can go on the roof of my Airstream and see what things (vents, antennas, etc.) have been caulked with the standard products; they’re drying out and starting to crack around the edges.  I will have to go up on the roof sometime, scrape all that stuff off, and re-caulk.  It’s not a job I’m looking forward to.

You can also see the things that were caulked with Vulkem or TremPro.  They’re still soft and pliable, even sticky, after years of UV exposure.  When I removed the old cellular antenna a couple of weeks ago, the caulk exposed to the UV was hardened but intact, and still waterproof. Around the base of the antenna the caulk was still gooey.  Think about that: the antenna was installed in 2005 and the caulk on it stuck to my fingers like fresh glue after eight years!  I’ve got it sitting here on my desk, just because I like to pick it up and marvel at it once in a while.  (Yes, that’s super-geeky but hey, it inspired this blog you’re reading.)

And eight years is nothing.  I’ve taken apart sections of my 1968 Caravel and found Vulkem contained inside joints and seams that was still good.   That Vulkem was probably decades old.

So that explains why I was willing to wait a week to get a tube of Vulkem 116 from an online seller. I used it to seal up the antenna hole for the cellular Internet booster.  The hole was 3/4″ and the cable was only 1/4″ so I used a set of rubber grommets to fill in the gap, plus a 2″ tall rubber “boot” that I found at Ace Hardware.  This formed a small tower on the roof, from which the new antenna cable emerges. Then I caulked the beejeebers out of the whole thing, sealing it completely.

IMG_2120Two days later, the caulk still feels like it was fresh from the tube, and since it cures very slowly (just 1/16″ of an inch per day at 75 degrees F & 50% humidity) I expect it will take at least a week due to our low humidity.  Fortunately, the Airstream isn’t going anywhere for four weeks.  I’ll get back on the roof in late May to check on the antenna cable again, after having towed the Airstream 2,000 miles to Ohio, just to confirm that the seal is flexing appropriately at highway speed and not developing any gaps that could cause a leak. I’m pretty sure it will be fine.

There are a few challenges with using this stuff.  First off, the fumes are stinky and toxic, which may be why it’s not approved for indoor use.  I would not use this in a workshop without having windows open and a fan.  Second, it’s trickier to shape and smooth than silicone caulk, because it sticks to everything.  The old “wet finger” trick that you use with silicone won’t work—it’ll stick to your wet finger.  I strongly suggest wearing disposable vinyl gloves when you work with it, and bringing along a bunch of paper towels for cleanup.

IMG_2116Third, saving the leftover tube is a bit of a pain.  It’s hard enough to obtain that you don’t want to lose the leftovers between jobs.  Some people put it in the freezer, which I think is a bad idea because the smell of the caulk can ruin your food, even through a plastic bag.  I like my ice cream to taste like Oreo Mint, not vanilla Vulkem.

We’re trying an experiment instead.  We wrapped the nozzle in plastic kitchen wrap, and then vacuum sealed the entire tube with Eleanor’s Food Saver.  (Eleanor wants me to mention that this was her brilliant idea, and I’m glad to do so.  If I open the tube in a year and find it congealed then it will be Eleanor’s terrible idea.  But it should be fine.)

Written by RichLuhr · Categorized: Airstream, Maintenance

Apr 21 2013

Replacing the Hehr window operators

I did warn you that the next few weeks would be mostly about Airstream maintenance, didn’t I?

The job list on the Safari is pretty long, so I’m trying to tackle at least a piece of a project every day.  The past few days Eleanor has been helping me with preliminary bits of the rest of the storage cabinets I started before our last trip.  We’ve figured out how we want to assemble the cabinet and glued up some trim pieces with aluminum strips, as Kyle and I did before.

I’ve also had the countertop made by a local wood shop. It’s black walnut, measuring about 18″ x 69″.  You might think that would be monstrously heavy, but I had it planed down to 5/8″ thick so it’s just 19 pounds.  Not lightweight, but reasonable for solid wood. We think it looks fantastic, even before final shaping and finishing, and I am really looking forward to seeing it finally installed. I’ll post pictures in a future blog.

One of Saturday’s little tasks was to tackle one of those common annoyances in the Safari-class Airstreams.  Those trailers used a type of Hehr window that opens at the bottom third of the glass.  The window operators (cranks) are made of cheap pot metal and they eventually strip and fail.  We’ve got two failed window operators in the trailer and a few others showing signs of imminent failure.  (You’ll know because you have to spin the window crank quite a while before it finally “catches” and starts to move the window.)

This is a job that the dealer will probably charge an hour’s labor to do, but you can do it yourself in less time.  The trick is finding new replacement window operators.  They’re called “torque operators” and they are Hehr part #008-192 if you’ve got the window knob on the right (as seen from inside the trailer).  I found them online for about $8, and bought three figuring that we’d need a spare soon.

Replacing the torque operators only requires two tools, a Philips screwdriver with a narrow handle and a regular (flat-bladed) screwdriver.  The job is a little tricky, and I was wishing someone would document it, so photos are below to illustrate most of the steps. In short:

  1. Inside the trailer, open the window fully if it still works.  Remove the black knob by removing the screw in the center.
  2. Outside the trailer, remove the two small black screws in the hinge just above the movable part of the window glass.
  3. Open the window (if it didn’t operate by the knob) and pop out the C-clips on the arm hinges (one on each arm).
  4. Pop the arms apart using the flat bladed screwdriver (one on each side).
  5. Now you can lift the window all the way up and either pop it out of the hinge or slide it sideways until it comes out of the hinge.
  6. Again using the flat screwdriver, pry the lower end of the spring off the upper arm so that the arm can move freely.  Be careful not to puncture the screen with the spring.  Do this on each side.
  7. On the right side, remove the screws that hold in the mount for the round bar.  The top one will be hard to get to, so this is where the narrow handle of your screwdriver is crucial.
    replacing Hehr window operatorOn the left side, remove the three screws that hold in the torque operator.  Again, the top one is a pain to get to.
  8. Drop the round bar down on the right side, then the left.  It should come out now, with the torque operator attached.  Might take some wiggling and cursing.  Don’t let the springs and arms fall off, because that will just make your life harder.
  9. Remove the torque operator and note what a piece of crap it is.  Scratch your head and wonder why they didn’t make it out of more durable material.
  10. Replace with a new torque operator, and wiggle the whole assembly of bar, springs, arms, and operator back into place.
  11. As they say, “installation is the reverse of removal.”  Riiiiiight.

Getting the top screw back in on each side is a pain. I taped the screw loosely to the driver and that helped, or you could use a magnetic bit.  Getting the window back in the hinge is a hassle too.  It takes a little force.  A helper would be useful here, although I managed to do it myself in a few minutes.  The rest is pretty easy.

I’ve still got one more torque operator to replace on the other side, but with the Airstream in the carport I can’t get to it right now.  That will be an on-the-road repair sometime in May or June.  The third operator will sit in the box of spares until the Window Failure Lottery is complete and we have a known loser.  And now we can open up a window in the bedroom and let in the air again!

 

Written by RichLuhr · Categorized: Airstream, Maintenance

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